The Good, The Bad and The Ugly

Fortunately, my website is filled primarily with good news stories. There are a few bad news posts but I think this is my first entry that falls under the heading of just plain “ugly!”

Back in November I did something really stupid. I have lots of rationalizations to explain how this “ugly” event could happen; however, none of them really matter. The bottom line is that I raised The Bloody Beast on the garage lift while the bonnet was propped up and it lost the battle when it struck the garage ceiling. This is the nice fit I achieved following the encounter with the ceiling.

Bonnet Damage

Bonnet Damage

After a generous display of profanity and tears, I pulled the bonnet off the car and drove it to Virginia (a 30 hour round trip journey) to Maple Hill Restorations and my friend Jeremy Turner. Jeremy specializes in Shelby 350 restorations but he took on my Healey twelve to thirteen years ago and completed all of the bodywork and paint. As far as I was concerned he was the only person who should try to “fix” my big mistake.

He could not get to the repair until early June of 2020, but it was worth the wait. This is an image of the bonnet after it was straightened and painted.

Bonnet Painted at Jeremy’s Shop

He is a magician! Beautiful work. So, following another quick trip back to Virginia I re-installed the bonnet on the car with little drama and now all is right with the world – well at least the Healey world!

To avoid any issues with damage to the front shroud or the freshly painted bonnet I placed my Healey shroud quilt over the front of the car and placed a 2 x 4 across the engine bay.

Preparing to Fit Bonnet

With the assistance of my wife, I was able to re-install the bonnet on the hinges and after some fettling and tinkering I was able to adjust it to end up with nice gaps all around.

A helpful tip I picked up from one of the Healey forums to help with bonnet alignment is to place a piece of tape over the bonnet striker catch and then put a little paint (or finger nail polish) on the tip of the striker pin. Once you see where the pin is hitting the tape you can adjust the striker assembly to re-orient it until you have it lined up in the center.

Bonnet Striker Pin

Bonnet Striker Alignment

 

Repaired Bonnet Installed

Repaired Bonnet Installed

Repaired Bonnet Installed

Repaired Bonnet Installed

The wounds have now healed with a big “thank you” to Jeremy! Now I am back on the road again.

On the Road Again

All of this called for a little celebration with the good stuff!

A Little Celebration

Chapter 87 Week Fifty-Seven January 14, 2008

The windscreen was a very tight fit! I suppose that it should be to minimize leaks, but it took some tugging on a drift through one of the lower mounting holes in the stanchion and a lot of pushing to finally get the uppermost capscrew to thread into place. The RH side didn’t require any shimming, but the LH did. You do want to make sure that there is no undue force on the stanchions or you might end up with a broken glass! I added a little 3M caulk strip under the post pad seals and between the windscreen frame seal and the post pad. I decided to run the seal under the post pad, though consulting with the “experts” resulted in at least three ways to do this job: under the pad, between the pad and the post, and cut off flush with the pad. I am using post mounted driving mirrors from Cape International, so they were mounted at this time and tightened through the posts.

Windscreen and wipers installed

Capesport Mirrors

After finishing the windscreen, I fixed the original “rainbow” wipers with new rubber to the wiper posts and following the addition of some windscreen washer fluid to the parcel tray mounted fluid reservoirtried out the wipers. All worked fine, including the intermittent wiper rheostatand electric washer pump I has installed previously. The kit from Ed Esslinger also turns on the headlamps when the wipers are activated – a requirement in many states now. 

Next was the installation of the bonnet. I first removed the striker pin assembly so that I could have the bonnet lie flat in the surround. Four 1/4” bolts with the heads to the outside are used to fasten the hinges to the bonnet hinge brackets. This process took some adjusting to get things right and at least one assistant is essential! After getting the bonnet lined up I re-secured the striker pin assembly to the bonnet and adjusted it and the bonnet latch support bracket to align all. The anti-rattle spring was then connected to the hood latch remote control rod and the bonnet release mechanism was tried with success.

Bonnet Latch Assembly

Strike Pin Assembly

Bonnet down

Bonnet Up

 

Chapter 26 – Cleaning and Trial Fitting

September 12, 2005

Jeremy Turner Begins His Work 

 We took the car to Jeremy in April, but he got stacked up during the summer months with the work of previous customers who wanted a few things done to ready their cars for shows of various types. Unfortunately, that meant pushing the BT7 off to the Fall.

To Maple Hill Restorations 1

Maple Hill Restoration Arrival 1

This week Jeremy got to work. First he media blasted and painted the seat backs and frames so that they could be sent to Heritage Upholstery for finish upholstery work. After I get Rick Kiser to build a new rear seat squab I will be ready to begin the waiting process for the interior work. I expect at least 2-3 months for that job.

Jeremy began by fitting the doors and wings. Not as easy as it might have been since I am using new aluminum wings that don’t fit quite as nice as the originals, but the originals were consumed by rust. The bonnet had two holes punched in it for the installation of hood locks and we agreed that the holes needed to be filled. He cut the reinforcing frame off of the back of the bonnet to blast any rust from the skin, welded the holes closed and primed.

Latch brace removed_4

Underside of hood rust_7

Outside of latch brace repaired and cleaned_6

He also bent back the skin on the bottom of the doors to again get all the rust blasted out and primed. This will alleviate problems in the future. It is all a slow process, but it is what must be done to end up with the quality job I want!

Rust exposed on bottom door edge_4

Door edge lip pulled out to expose rust_3

Door edge glassbeaded to remove rust_2

Door edge epoxy primed_1

I received the windscreen frame from Custom Chrome Plating in PA. It was a beautiful chrome replating job. It should have been for $500.00 for four frame pieces! I took it and glass and hardware to Village Auto Center in Harrisonburg for assembly. I am nervous about their care, but I expect everything will come back fine.

September 20, 2005

The windshield came back and was nicely assembled except the corners don’t meet as tightly as they need to to prevent leakage. I will work on that later before final assembly. I put the pillars on the frame and will take it to Jeremy for fitting to the body.

Jeremy sent some new images of his latest work that focused on cleaning up the bonnet, fixing a dent and filling the lock holes.

Rear hood brace removed_4

Hood pin holes being welded_6

Screw holes welded up_2

Right hand hole welded up_1

Left hand hole shut up_3

Rust cleaned from underside of hood and dents removed._3

Body work done on underside of hood in areas that would be hard to get to when the braces are welded into place

Rear hood brace removed_4

Trunk brace removed_6

Trunk braces cleaned_8

Underside trunk lid cleaned

December 10, 2005

I have been disappointed that after a good start in September, Jeremy began working on other projects and didn’t make much progress with the Healey. He got back to work after Thanksgiving and forwarded the following photos of work done on the boot lid. It was badly deformed, cracked on the top side edges and didn’t fit the shroud particulalry well. I was pleased to see his skill with cutting and welding. Things are looking up!

adjusting LH trunk gap_4

adjusting RH trunk gap_5

new trunk edge to adjust gap

trunk edge removed

epoxy primed latch brace

underside epoxy primed

aligning the door and quarter gap

February 19, 2006

Rear lights on Healeys leave something to be desired. I came upon a web site that offered a good idea for adding some rear illumination without any obvious physical modifications. It involved converting the rear reflectors to working lights using a pair of 10 watt,12 volt MR11 halogen bulbs that I found at a local lighting store. I also ordered two connecting terminals on-line since the connectors are very small and somewhat delicate pins.

As per the directions on the Healey Club of Ontario web site, I removed the rear reflectors from their pods. I dicovered that this works with the original reflectors but not with those currently available! The reproductions are not as deep and do not have the foil reflector. The easiest way is to carefully insert a small screwdriver between the chrome bezel and the rubber ring. Pull the chrome bezel off, remove the red reflector, and the rubber body will easily pull out of the hole.

I removed the silver foil from the reflector and drilled a 1″ hole in the center of the rubber grommet. I then trimmed the hole to create an
inward taper into the reflector body to match the cone of the new bulb. Then I secured the red reflector to the grommet, sat the halogen bulb inside and pressed the assembly together. This is not real easy to do. I added a little dishwashing soap to the rubber to make it simpler to press things together. After assembly, I used a bead of silicone to seal the new bulb to the rubber grommet.

After installation on the car, run wires from the two brake light terminals in the trunk to each reflector pod and from the wire ground screws on each side to the same pod. The bullet connectors for the brake lights are in the boot on the driver side at the rear. I used bullet connectors and changed the single bullet holders to double so I did not have to spice into the wires. Driver side is White with Purple trace and Passenger side is White with brown trace. Since these will
light both with brake and turn signals this is important.

Rear modified reflectors 2

Rear modified reflectors 3

Rear modified reflectors 4

Rear modified reflectors 5

Halogen bulb